Dyno result, can't get any worse.
I went to the dyno on Saturday and in all it was a huge disappointment. Here's the set up:
CRX with b18a with t3t/t40e at 7psi spearco fmic DSM blue top Walboro pump 2.5" to 3" exhust hks ssq bov TurboEdit Delta wg. NKG brk7e (sp?) gapped at 32 Far from my expectation, i put down 148hp on a dynojet, it is beyond lame. The biggest problem is my ignition, it was misfiring like mad at high rpm, no matter what we did, it still did the same thing. I used PM7_NG26 with stock pr4 map imported, then I had 120% fuel adjusted for boost with -.60 retard. At first it was running lean at 14:1 at WOT. We ajust things a bit and got the AF somewhat stable. I'm going back again next sunday when they have a mechanic there. I'm suspecting the dizzy has been messed with and it is not at stock timing, i believe the owner of the engine before me had mess with the timing. Anybody got any input? |
Re:Dyno result, can't get any worse.
What was the torque number?
Something seems amis, you should be putting down alot more hp than that with that setup. Get that ignition ---- checked out. |
Re:Dyno result, can't get any worse.
Use stock spark plugs gapped at .040, replace your distributor cap and rotor, and make sure you have good wires installed as well.
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Re:Dyno result, can't get any worse.
Yeah that sounds like wires or dizzy problems. Go time it back to stock and the change around your timing on turboedit. All you need is a timing light.
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Re:Dyno result, can't get any worse.
dont forget to check ignition module. i had that problem and it turn out to me the igniter
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