Dyno result, can't get any worse.
#1
Dyno result, can't get any worse.
I went to the dyno on Saturday and in all it was a huge disappointment. Here's the set up:
CRX with b18a with t3t/t40e at 7psi
spearco fmic
DSM blue top
Walboro pump
2.5" to 3" exhust
hks ssq bov
TurboEdit
Delta wg.
NKG brk7e (sp?) gapped at 32
Far from my expectation, i put down 148hp on a dynojet, it is beyond lame. The biggest problem is my ignition, it was misfiring like mad at high rpm, no matter what we did, it still did the same thing. I used PM7_NG26 with stock pr4 map imported, then I had 120% fuel adjusted for boost with -.60 retard. At first it was running lean at 14:1 at WOT. We ajust things a bit and got the AF somewhat stable. I'm going back again next sunday when they have a mechanic there. I'm suspecting the dizzy has been messed with and it is not at stock timing, i believe the owner of the engine before me had mess with the timing. Anybody got any input?
CRX with b18a with t3t/t40e at 7psi
spearco fmic
DSM blue top
Walboro pump
2.5" to 3" exhust
hks ssq bov
TurboEdit
Delta wg.
NKG brk7e (sp?) gapped at 32
Far from my expectation, i put down 148hp on a dynojet, it is beyond lame. The biggest problem is my ignition, it was misfiring like mad at high rpm, no matter what we did, it still did the same thing. I used PM7_NG26 with stock pr4 map imported, then I had 120% fuel adjusted for boost with -.60 retard. At first it was running lean at 14:1 at WOT. We ajust things a bit and got the AF somewhat stable. I'm going back again next sunday when they have a mechanic there. I'm suspecting the dizzy has been messed with and it is not at stock timing, i believe the owner of the engine before me had mess with the timing. Anybody got any input?
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12-07-2004 08:58 PM