Engine misfiring after 5500 rpms
Well Since I took out my cat it free'ed up some back pressure and now I am able to hit 8psi when I changed my external wastegate. After I go past 6 psi say 6.5 around 5500 RPMS or there about it starts to sputter/misfire, I am burning full rich and EGT's are normal, my plugs are 2 ranges colder, no CEL's and timing retarded 0.5 deg per psi with my BTM. I don't apperar to have any vacum leaks that I know of. checked plugs and are normal tan color.
Any suggestions on what is causing this?
Any suggestions on what is causing this?
Originally Posted by AbaZ
Turn your BTM down to 0 and see if it goes away..
Jeff
Jeff
Also when it does misfire it is at full or close to full throttle, and when it pops my A/G goes totally lean and comes back to rich again. The car does not buck or anything like that, I am leaning towards spark as the problem, but I guess i have to start somewheres.
Thanks
Mike
well I think I may have figured it out, my a/f guage is so in accurate, after I gapped the plugs to .032" it ran a little better. I had a hunch that I was leaning out so I tryed a friends A/F guage and once we hooked it up it was so evident, I was leaning out when I was at full throttle, My FMU is djustable luckly and i adjusted it to the max it could go which is probly 7:1 or so (6:1 disc) and I am good till about 8ish PSI and it starts to lean out again and sputter , I am going to change back to my lebaron wastegate (5.5psi) and run about 6-7 just to be safe. Once I ged bored with this turbo and get a bigger one I will get a hondata.
I am running NGK ZFR7F-11, and the popping is gone, I was hitting almost 10 psi yesterday and no popping
was fuel problem, luckily I caught it, even though I got a spare engine still would hae made uneccessary work.
was fuel problem, luckily I caught it, even though I got a spare engine still would hae made uneccessary work.




i run ngk 3330's aka bcpr7es @ tehir stock .32 gap and 14psi and no popping hwat so ever